Meet 1 Success

Today in Meet 1 we finished in first place and went undefeated. This was thanks to our consistent autonomous and hours of driver practice, although we did fail to hang one match due to driver error.

Overall, today was a satisfactory day, we still do hope to drastically improve our robot for the next meet by being able to score in the lander. We were not able to do that this meet because we found that we needed a much larger gear ratio in order to lift the arm, something we were not capable of implementing due to how close meet 1 was.

Suit Bots matches from meet 1